Showing posts with label bobbin case. Show all posts
Showing posts with label bobbin case. Show all posts

Saturday, 10 November 2018

Singer 411G stitching issues

I bought this machine on the price alone, and thought I'd start by cleaning it. After cleaning it wasn't stitching well, so I assumed (correctly) that something I did had caused it to go out of balance.
The 411G has gold accents
The symptoms were that threads were nesting badly in the bobbin area. After perusing the 401 service manual thanks to Sewing Dude (https://sewingdude.files.wordpress.com/2012/09/singer-401-service-manual1.pdf page 131), I decided to go through and check the clearances for the bobbin case (which seemed very loose even before I cleaned it) and anything else in the bobbin area.
So this is the procedure:
Remove the needle, remove the presser foot, slide the slide plate (1) back, lift and remove the stitch plate (2).
If you want to (it's not necessary) you can also remove the slide plate. It's just like the 66 and 99. Put down the platform that holds the stitch plate then slide the plate back until it clears the spring.
You should now see this (without the arrows of course)
You will need a set of narrow feeler gauges to check the clearance. If you don't have any, you'll need to get some or guess the gap.
Narrow feeler gauges
Using the picture with the arrows, check the gap marked 1. It should be 12-14 thousandths of an inch (thou). If it's not in that range, go on to check 2, the vertical clearance between the hook and the spring, 16-18 thou. These are both adjusted at the same time, by loosening the two screws marked by thick white arrows and moving it until the clearance is right, then re-tighten the screws.
Once you've done this, check 3, the distance between the bobbin case and the spring. If this is not between 12 and 14 thou, adjust it. The adjustment is easy, but you first need to remove the machine's plastic base (two screws), exposing the locking screw (see picture below).
lock screw for adjusting bobbin case clearance
Once you've loosened it, you can turn the screw to the right of the bobbin spring (see below) which is eccentric and will increase or decrease the gap. 
Once this clearance is right, perform a test sew. My machine was made to sew at full speed with a very narrow stitch length and making a pattern, the ultimate test. It didn't skip any stitches or even hint of bunching up. Machines like this that do everything are a lot more complex than, say, a 15 or 201 so they need more attention and are harder to get to, but with the right resources (mostly just knowledge) you can keep them in top condition. 
Another problem was varying speed during sewing. This means that the foot controller's carbon pile needs a clean. This is a horrible job, so I replaced the controller. Later on I pulled out a Japanese electronic controller I've had for a few years and that was even better, because apparently you can leave these plugged in without any heating (the 411's controller was also quite hot when I changed it). The electronic replacement required a little soldering.
It's now almost perfect. The last job is to see why the motor is noisy. A drop of tri-flow was suggested on another blog, but it hasn't quietened it, so I'm thinking I'll have to remove and disassemble. Not a job I'm looking forward to, since it's completely enclosed, but I'll do it and let you know of any obstacles.

Monday, 8 September 2014

Singer 320K2 bobbin case mod

Don't you love a mod? Ah the '60s... No that's a different kind, but this one's more useful than stylish.

Here is the bobbin case after Nick Ciancio did his thing:

The arrows point to the bit he machined off. I asked him to explain the mod and he said that when there's a 15x1 needle inserted, there's no problem when straight stitching. When zig-zagging, however, there's a real danger of the needle hitting the bobbin case, and the removed section marks the point of impact. The longer 15x1 goes down an extra 2mm or so and removing this by making the "U" shape a little wider (see arrows) removes the possibility of impact.

I now have an extremely rare old machine that has a free arm and uses common 15x1 needles! Allowing a 15x1 needle to punch the metal out is a bad idea. Just Google for the result and you'll find pictures of destroyed cases.

I'm more than happy to recommend Nick to anyone in Melbourne who has a vintage machine. He's very friendly, can repair anything and really loves the old machines.

Oh and I should mention that in a comment on my last post I said that I was a little disappointed in the 320s stitch quality. Checked the needle height and it was a mm or two out, which had also put the timing out. Spent 20 minutes fixing it and she sews much better now.